The sides of the carriage are slightly slanted
so during production, the piece can be popped out of the mold. The left side of the
carriage required milling so the mounted split-nut would be perpendicular to the lead
screw. There is a small ledge that the split-nut subassembly mounting plate's top edge
rests against. All milling & drilling was performed using the lathe to assure
alignment, especially of the two, lead screw holes (make sure to clear the eccentric for
the pinion gear). I borrowed a Taig lathe
carriage because, of course, you need two to do the operation. To perform the milling operation, I used a solid carbide, two-flute (for
soft materials, use a 4-flute for hard materials) 5/16" finishing end
mill. I have also used a
fly
cutter to mill a carriage. De-burr
the dovetail edge where it was milled. Check the entire carriage dovetail for burrs
leftover from manufacturing. A dab of kerosene allows a smooth cut on aluminum. This
mod was performed
before I had either the Taig
or the RF-25 mills.
Removed all calibrated dials, glass bead blasted
them (sandblasting too aggressive/coarse), then using the lowest lathe rpm, smoothed
the scale with 220, 320 then finally 400 grit sandpaper. Do not be too aggressive or you
can remove the markings. This method only works for dials that have deep marks to begin
with. Indicia will be finer & the knob looks nice when the rough machine marks are
removed. Careful, the dials are factory Loctited on & screw off (not pull). I put two
small flat sides on the non-threaded area of the lead screws for a very small, open-ended
wrench to facilitate disassembly/assembly. Grease (not white lithium) makes these knobs
work very smoothly. The two ends of the movable dial scale zero (the ¾ circumference
spring clip in the dial bearing block grove) may be rough; remove & grind the ends
flat. Go to OEM vise for a close-up photo
Replaced all of the OEM dial brass spinner pegs
with a pivoting-type (Wm. Berg) as per
MIL-STD-1472. This one change alone greatly enhances the smoothness of operation & is
the least expensive modification for the largest increase in machine performance.
Remember, that when
tapping
the steel knob, the tap hole is (larger) for 50% threads not 75% like for softer
materials. Always drill the exact recommended tap hole for maximum thread strength. Grease
on the stainless steel pivot screw makes it smooth. A small nylon washer, just the size of
the pivot screw body, 3/16", (not the thread itself) removes the last of the in-out
play of the aluminum spinner knob. I also filed two small flats on the eccentric for the
pinion gear, just behind the knob, to accept a miniature 5/16" open-end wrench. This
greatly facilitates rack & pinion engagement adjustment.